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Enthusiast ![]() Joined Sep 22, '10 From pomona, ca Currently Offline Reputation: 1 (100%) ![]() |
hey whats up guys, once again i have ran into another issue. this past weekend i was doing some tuning on my car and i wanted to UP the boost a little bit more, but to my surprise i cant go past 11psi......
i did another boost leak test and my intercooler pipes( inlet to outlet) hold 15psi without trouble and the pressure stays pretty steady....so no mo major leaks there... i got a cheap MBC when the MBC is closed i boost 7spi which is the wastegate spring load MBC half way open = 11psi fully open = 11psi if i remove the boost controller and leave the hose that connects to it by itself, still get 11psi............. so i im assuming i must have a leak somewhere past the throttle body...im not sure how to test the intake manifold and all other vac lines to see if i got a leak there under pressure, because in idling i sprayed starting fluid around injectors, manifold, ects. and idle didnt change. or is it possible that my EGR could be leaking??? any help is appreciated |
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Enthusiast ![]() Joined Sep 22, '10 From pomona, ca Currently Offline Reputation: 1 (100%) ![]() |
C'mon guys, im sure somebody knows how to truouble shoot this issue
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![]() Enthusiast ![]() ![]() ![]() ![]() ![]() Joined Jan 4, '12 From US Currently Offline Reputation: 6 (100%) ![]() |
How do you know you're boosting 11 PSI?
Boost gauge or data log? -------------------- 1993 Celica GT Coupe - sold
1994 Celica GT Liftback |
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Enthusiast ![]() ![]() ![]() ![]() ![]() Joined Dec 8, '03 From Lancaster CA Currently Offline Reputation: 6 (100%) ![]() |
you are flirting with disaster at that high a boost. i dont think i went much over 10. its been so long, i just cant remember
-------------------- 2001 Celica GT-S Turbo
1997 Supra TT 6speed 1997 Celica 3MZ/1MZ swap 1990 Celica All-Trac |
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Enthusiast ![]() Joined Sep 22, '10 From pomona, ca Currently Offline Reputation: 1 (100%) ![]() |
I got no signs of detonation, or knock wat so ever and im a,little on the rich side on my afr (11.5} im using my boost gause to check my psi. Today I disconnected the line going to thee WG and still 11psi... What the heckk is going on .....boost should have gone way up!
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![]() Enthusiast ![]() ![]() ![]() ![]() ![]() Joined Jan 4, '12 From US Currently Offline Reputation: 6 (100%) ![]() |
im using my boost gause to check my psi. Boost gauges can go bad. I bet that's your problem... -------------------- 1993 Celica GT Coupe - sold
1994 Celica GT Liftback |
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Enthusiast ![]() Joined Sep 22, '10 From pomona, ca Currently Offline Reputation: 1 (100%) ![]() |
The booost gauge is still pretty new. If it was bad at least I would feel the extra power. Ive been searching other forums and I got the idea that my exhaust might be too small. Alll my exhaust is 2.25" starting from the downpipe
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![]() Enthusiast ![]() ![]() ![]() ![]() ![]() Joined Feb 11, '08 From Auckland, New Zealand Currently Offline Reputation: 0 (0%) ![]() |
what turbo? wastegate door being blown open?
-------------------- Mike W
1996 Toyota Celica ST205 GT-FOUR GT2860RS turbine, TiAL mvr44, JE 86.5φ piston, Clutchmasters FX400, APEX P-FC 269awhp / 273ft-lbs |
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Enthusiast ![]() ![]() ![]() ![]() ![]() Joined Dec 8, '03 From Lancaster CA Currently Offline Reputation: 6 (100%) ![]() |
it could be the exhaust. it might be too restrictive causing it to prevent the turbo from spooling more.
-------------------- 2001 Celica GT-S Turbo
1997 Supra TT 6speed 1997 Celica 3MZ/1MZ swap 1990 Celica All-Trac |
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Enthusiast ![]() ![]() Joined May 30, '05 From MN Currently Offline Reputation: 8 (100%) ![]() |
Sounds like wastegate problem. It might be stuck open or the arm moving easily. GL.
-------------------- 3sgteing.
..burns twice as bright, lasts half as long. "The weight of the world is love. Under the burden of solitude, under the burden of dissatisfaction." -Allen Ginsberg- |
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Enthusiast ![]() Joined Sep 22, '10 From pomona, ca Currently Offline Reputation: 1 (100%) ![]() |
i think i found my problem, i was checking the car while it was on with a hose to my ear trying to listen around injectors, TB, etc. and i heard hissing sound coming from the back of my throttle body right by the IACV....that might explain why my idle would not go lower than 1100rpm without retarding timing..... im gona fix that leak today and hopefully i should be boosting a little better. thanks for the replies
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Enthusiast ![]() Joined Sep 22, '10 From pomona, ca Currently Offline Reputation: 1 (100%) ![]() |
So, I fixed the leak on the throttle and still have the same problem. I even tied the wastegate arm with a wire to keep it from opening. I don't know what else to try. .
Maybe I'll upglsize the downpipe this week to see if that helps... any other thoughts? |
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![]() Enthusiast ![]() ![]() ![]() ![]() ![]() Joined Feb 1, '05 From Charlotte NC Currently Offline Reputation: 14 (100%) ![]() |
did you ever find the issue? im begining to think im having a similar problem....
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Enthusiast ![]() Joined Sep 22, '10 From pomona, ca Currently Offline Reputation: 1 (100%) ![]() |
it turns out it was my wastegate arm. it was some what at an angle and even though the flap seemed closed it remained a little open.
i had tried holding the wastegate closed with a wire before and i had the same problem, only boosting 11 psi, but the wastegate arm was still connected...... i completely removed my wastegate and tied the flap closed again with a wire; when for a spin and shot all the way to 15psi. thats how i knew the arm was at an angle keeping the wastegate a little open. soon after that i noticed my turbine wheel was chipped...i had no filter so most likely something flew in and broke it so i got myself a new turbo, a i correctly positioned my wastegate...and this time i went with a 50 trim instead of the 57 and boosting around 14 psi and i get spool at 2500RPM and get full boost at about 3k RPM =] happy camper! lol |
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![]() Enthusiast ![]() ![]() ![]() ![]() ![]() Joined Feb 1, '05 From Charlotte NC Currently Offline Reputation: 14 (100%) ![]() |
thats good to hear!! i checked my wastegate and it too seemed closed. i havent took my entire wheel out (as my turbo/manifold is one piece) but i have to figure out something... im not getting any boost at all...
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Lo-Fi Version | Time is now: June 18th, 2025 - 6:28 PM |