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> My 3s-gte Thread, rebuild project (pics) Done!
post Jul 24, 2006 - 5:06 PM
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95celgt



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Hey every one, this is my thread dedicated to the 3sgte in my car.
Im making one thread for all the projects that will be done to the motor itself.

Info: Since I bought the car from Chanh55, I was wondering why it was not performing as it should, I did various tune-ups, only making marginal difference.

The biggest project I did up to this point on this motor was when i took out the piping and FMIC to clean it out(this made a huge difference BTW). I addressed this due to massive blow-by coming out of the valve cover PCV pipe. clean up project

Well after that, I decided to check compression and the numbers were as follows: 180:170:95:180
As you can tell my #3 cylinder is gone for some reason....so the tear down began:

Stage 1:
Bolt on accesories taken off(TB,ALT, FMIC stuff, etc.) as well as harness plugs.
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radiator out
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turbo and manifold out (this was probably the hardest step lol)
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Head off:I had to go to pep boys to get the t-55 hex bit for the wierd toyota head bolts.
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This post has been edited by 95celgt: Sep 25, 2006 - 12:06 AM
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post Jul 24, 2006 - 5:09 PM
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presure2



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just for future refrence, the toyota 3sgte head bolts are triple square 12mm sockets.
the tool looks like this:

good job so far!


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post Jul 24, 2006 - 5:12 PM
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playr158



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A+ work bro....the way it looks i'm thinking a ringland is gone bye bye
post Jul 24, 2006 - 5:16 PM
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95celgt



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Well, i'm a bit relieved to find out the exaust valves on cylinder 3 had a bad seat, which may have been the cause of the low compression. So I have taken the head to the machine shop for a valve job, the head itself is pretty perfect, showing no signs of warp. I ordered a complete head gasket set as well. lets hope when i put it back together it runs like the demon it should be:).

BTW: The car always never hit over 6 psi, the acuator was capped off when i got it so i reconnected it to the vsv but no dice... should i get another?

Any mods i can do to the TVIS for gains? what would happen if i removed the butterfly's?

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this is cylinder 3, does it look like its in good shape?
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post Jul 24, 2006 - 5:34 PM
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presure2



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take some nice high-res shots of the cylinder walls, and look at them on your puter...thats how i found this:
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if you can feel them with your finger nail, the wall is toast from what ive read.


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post Jul 24, 2006 - 5:54 PM
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lagos



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keep up the good work.


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post Jul 24, 2006 - 6:21 PM
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Defgeph



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Awesome thread man. Sorry about your motor, keep us updated !!!!!


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post Jul 24, 2006 - 8:48 PM
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95celgt



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I just took a bunch of pics of the walls and didnot see anything, i felt around the walls and they feel really smooth.

I just dont know if I should continue into rebuilding the bottom end.
I dont want to slap on the fresh head and then have to tear it apart all over again, so im wondering if I should just do it while everything is out "just in case".

notice the fully labeled harness rolleyes.gif
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some wall shots
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post Jul 24, 2006 - 9:01 PM
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95celgt



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If the ringlands were blown, wouldn't the car smoke a bit?
When i run the car, it NEVER smokes, even past 6K rpm.
post Jul 25, 2006 - 12:36 PM
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Chanh55

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Wow good work man. Did you ever get the speedo to work?
post Jul 25, 2006 - 1:34 PM
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95celgt



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im doing that as well, since theres more room with out the head in there:) i bet you knew this would happen all along lol.
post Jul 25, 2006 - 9:14 PM
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yungazzdriver



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well i could have sworn i used 10mm socket for the head bolts??? but uhm yeah you should look into the ringland problem 3sgte's are known for this thus being the reason for my rebuild but luckily my block is GREAT!!! because i took it to the machine shop for a quote and cleanin and pics will be up soon,.........highly recommend changing water pump and oil pump timing belt etc while you at it that is and well get it balanced, apr head studs and well build a MONSTER!!@! muahahahah
post Jul 25, 2006 - 11:48 PM
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95celgt



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Yup, decided to do the whole thing today, im taking out the rest of the block tommorow.

Stopped by the shop today, saw the head all cleaned up.

Told them i'll be back by the end of the week to deliver the block.
Im gonna use king bearings, new pistons, rings, rods, they are gonna polish and balance the crank, the whole 9 yards.

post Jul 26, 2006 - 8:40 AM
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playr158



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if your rods are in good shape might i suggest having them shot peened as a method of spending wisely...stock rods are good for about 400whp

but wat components are you planing to run (ie brand, size)
post Jul 26, 2006 - 10:17 AM
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zipstrips

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looks to me like the piston in the last picture is chipped in the left corner, right near the valve releif... good thing your gona go the bottom end!
post Aug 17, 2006 - 1:18 AM
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95celgt



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Hey guys, I havent updated as I have been really busy both with this project AND the 4agze swap for the AE86, i had delivered the block, they tore it apart by the next day, showed me the broken #3 piston, and honed block.

The head has a sweet 3 angle valve job biggrin.gif

I had them bore the cylinders 20-over, order all the parts, except the oil pump, i ordered that myself and saved a 100 bucks or so. new bearings, bigger pistons, rings, etc...I truly regret not taking my camara for pics.
I only took one of the short block with my RAZR mad.gif

I should get the entire long block back soon smile.gif
IPB Image
post Aug 17, 2006 - 6:50 AM
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playr158



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very nice..glad your project is coming along well smile.gif
post Aug 17, 2006 - 11:59 AM
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95celgt



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Hehe, thanks playr.

Some FYI for the readers....

Take the crank pulley/harmonic balancer off the motor BEFORE you start tearing apart the block, UNLESS you pave power tools like the impact gun. This way you can take off the timing cover, these two things deprived me of the clearance for the bellhousing to clear the clutch pressure plate, so i spent hours trying to squeeze the block down under the car, so that i could place it in a verticle position to take it out. It was the only way i could get it out with the tranny still in there.

Over all it was pretty simple, but just time consuming. I have the dash peices dissasembled as im STILL trying to get the speedo to work.

I was also gonna take this oppertunity to stick the a/c condensor and hard lines back in, but once i was aware that the wiring had to be modified for that as well, I kind of gave up on that hope....this decision may lead me to having to look for another car due to the constant 100+ degree temps here(even in the evening), but more on that later.
post Aug 17, 2006 - 2:05 PM
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lagos



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QUOTE
I was also gonna take this oppertunity to stick the a/c condensor and hard lines back in, but once i was aware that the wiring had to be modified for that as well, I kind of gave up on that hope....this decision may lead me to having to look for another car due to the constant 100+ degree temps here(even in the evening), but more on that later.



the wiring is very easy. i posted up a whole how-to on it.


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post Aug 17, 2006 - 2:41 PM
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95celgt



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well then....I MIGHT just keep the car;)

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