Oct 23, 2013 - 3:38 PM
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Enthusiast ![]() ![]() Joined Jan 12, '09 From State College, PA Currently Offline Reputation: 1 (100%) |
Hey guys,
Well it's been a while since I've been active, reason being I sold my old 1995 GT hatch in 2010. I changed locations to a more urban environment and the wife and I decided to get rid of the Celica and the 1999 Civic. We opted to get a 2010 Ford Escape V6 4WD so we can transport friends in comfort, and haul more junk in the trunk. Last year (after racking up 67k miles on the Escape), we traded that in for a 2012 Hyundai Santa Fe. As with the Escape, it is a V6, but the 4WD option again killed off that third pedal that we both enjoy using. As our financial situation improved through some inheritance, I got the itch for a 3rd pedal daily driver that I could eventually transform into a track car. After looking around at primarily late 90's BMW's and a few other options, I happened to look back to this forum for nostalgic reasons. Although I wasn't specifically looking for another Celica, sometimes some things are just meant to be. So as some of you already know, I synced up with Supershannon77, and ended up purchasing her baby. Over the course of the next few weeks or couple months I will be fixing the car so it is 100% road worthy again. It runs and drives just fine.. it's just a bunch of little things it needs. It would be best characterized as the car needs "adjusting and polishing" more than "fixing". A new sensor here, a bad hose there, tightening up brakes and replacing brake lines, and so on... The car will be my DD to and from work once all that is complete, and then as time goes on the plan by around next summer is to start tracking it. Start taking out interior pieces as they're no longer needed, adding coilovers and strut supports, getting it fully caged... etc. Most of these things I can figure out myself or have an uncle who can pretty much work on anything mechanical blindfolded help me. However there were 2 pressing concerns that I couldn't come up with a simple explanation for when I was test driving the car so I would like the guru's here to bounce ideas... 1- We were running very low boost (5-6 PSI) on the test drive. After a little bit of driving around and getting a feel for the car, I needed to see how it would spool up and react to boost at higher RPM's. We were going about 15MPH, had the car in 2nd, and punched it. As soon as we hit 4000 RPM, we hit a brick wall. It felt like hitting redline, no other way to describe it. As soon as I felt it I immediately came off the gas. After that the car still ran just fine, still boosted (but I didn't run it past about 3000 RPM), no difference in engine character or funky noises... nothing. Anybody have an idea as to what the issue there could be? The cars knock sensor isn't plugged in, and the check engine light was on (code 54), however after bouncing some ideas off others last night they said it might be a problem in the ECU wiring? 2- Since the knock sensor wasn't hooked up I was closely watching the air/fuel gauge. As we hit boost (even at 5 PSI and I'm not sure that should matter), the car maintained a 14.5-14.7 ratio, as opposed to..... anything below 12. Even as I hit that wall at 4000 RPM it was still 14.5. Any guesses as to the problem there? I'm guessing its again an electrical issue however I can't diagnose anything right now because the car is in NJ and I'm in Pa and it will remain like that for another two weeks. I'm trying to get some ideas ahead of time so that when I do go there for the weekend I'll be able to dedicate my time to the car itself, and not necessarily seeking out answers to questions here and waiting for reply's. Thank you all, I'm happy to be a part of this great group once again, and I will have pictures and updates on this as they come. I figured I'd link to Shannon's original threads to keep the cars history intact both for myself and others if needed: http://www.6gc.net/forums/index.php?showtopic=69018 This post has been edited by cardshark525: Nov 6, 2013 - 7:51 AM |
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Dec 28, 2013 - 1:12 PM
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Enthusiast ![]() ![]() Joined Jan 12, '09 From State College, PA Currently Offline Reputation: 1 (100%) |
Short update for now.
Took it to a shop (primeperformance in Stanhope) and they cleared all the codes, replaced the knock sensor which was at fault, added 2 filters to the free vacuum hoses and some other minor work. On the way home from the shop it was nice to be able to fully boost and the car is... umm... quick. Have it running at 15psi and 2nd gear is pretty much useless once it spools up. So all of that was taken care of and car was running just fine. Then I get it home and park it, naturally look underneath to check for leaks, and there's almost a waterfall of nasty redish brown rusty fluid leaking from the back of the engine. Checked intercooler level and none was missing (good and bad). Check the radiator... and I can no longer see the fluid in there. I traced the leak to just underneath the throttle body, the only fluid line that's in any diagrams back there is a water line return and it seems that's where it's coming from. Future plans (maybe today) are to trace the leak 100% and see what's going on. However considering the color that the fluid is (it's reeeeally brown and rusty), I'm going to probably replace the radiator as well as all the hoses. Anyone have any recommendations or preferences for radiators/hoses? This post has been edited by cardshark525: Dec 28, 2013 - 1:12 PM |
cardshark525 Cardshark525's 1995 GT w/ 3SGTE swap. (from DD to track car) Oct 23, 2013 - 3:38 PM
Neon90424 With that low boost sounds like its in limp mode Oct 23, 2013 - 4:35 PM
cardshark525 QUOTE (Neon90424 @ Oct 23, 2013 - 4... Oct 23, 2013 - 4:43 PM
cheela I'm glad Shannon's car is in the hands of ... Oct 23, 2013 - 4:40 PM
Neon90424 I dont know but my car was stuck on low boost, was... Oct 23, 2013 - 4:51 PM
Syaoran My recommendation is to install an EMS if this is ... Oct 23, 2013 - 5:12 PM
richee3 The ECU wouldn't change the AFR's because ... Oct 23, 2013 - 5:44 PM
cardshark525 QUOTE (richee3 @ Oct 23, 2013 - 5:44... Oct 23, 2013 - 6:14 PM
cardshark525 Well after my father in law unhooked and reconnect... Oct 27, 2013 - 8:20 PM
cardshark525 This Friday can't come fast enough... It's... Nov 6, 2013 - 8:09 AM
cardshark525 So I just finished changing out the oil (yes the d... Nov 9, 2013 - 2:46 PM
Smaay the plugs go to the EGR VSV and EVAP VSV mounted o... Nov 9, 2013 - 4:08 PM
cardshark525 QUOTE (Smaay @ Nov 9, 2013 - 4:08 PM... Nov 9, 2013 - 8:12 PM
cardshark525 Well I looked at the level sensor and it wasn... Nov 10, 2013 - 9:39 AM
cardshark525 Like I said the code 54 still pops up, here's ... Nov 10, 2013 - 2:35 PM
supershannon77 If it helps I didn't get code 54 until I chang... Nov 10, 2013 - 6:56 PM
cardshark525 QUOTE (supershannon77 @ Nov 10, 2013 - 6... Nov 10, 2013 - 7:10 PM
playr158 lots a PB blaster on them lug nuts. Nov 11, 2013 - 10:11 AM
njccmd2002 or torch, or 3/4 inch titatnium drill bit. Nov 11, 2013 - 10:21 AM
cardshark525 Yeah I know. I'll probably end up replacing th... Nov 11, 2013 - 6:49 PM
cardshark525 Looked into the situation a little further.
This ... Dec 30, 2013 - 7:11 PM
playr158 Will the Megan Racing radiator work yes.
the real... Dec 31, 2013 - 12:40 PM
cardshark525 Well the car is finally home in PA. Will have it i... Feb 3, 2014 - 1:35 PM
supershannon77 Updates? How are things? Figure out the leak? Hope... Mar 22, 2014 - 9:33 PM
cardshark525 So.... I was in the middle of a paragraph on my ph... Mar 22, 2014 - 11:16 PM
Tigawoods QUOTE (cardshark525 @ Mar 23, 2014 - 12... Mar 23, 2014 - 8:25 AM
cardshark525 QUOTE (Tigawoods @ Mar 23, 2014 - 9... Mar 23, 2014 - 2:06 PM
Tigawoods HA! for you! I just took my car from PA to... Mar 23, 2014 - 6:13 PM
cardshark525 So it was finally a nice day today so I got to wor... Apr 12, 2014 - 1:54 PM
enderswift I cant really tell which part you're referring... Apr 12, 2014 - 4:15 PM
cardshark525 See how directly underneath the throttle body I pu... Apr 12, 2014 - 8:08 PM
cardshark525 Dear Diary...
On my way home from NJ right at th... Apr 23, 2014 - 9:58 AM
cardshark525 Previously stated problems have been fixed as of t... Apr 27, 2014 - 5:29 PM
cardshark525 So I ran into an issue today after a fantastic dri... Jun 7, 2014 - 7:54 PM
enderswift Common problem, especially with an aftermarket clu... Jun 7, 2014 - 9:01 PM
cardshark525 Got all my parts in and went to work today on fixi... Jun 22, 2014 - 3:52 PM
cardshark525 Code 54 popped up again. Got pissed off, went thro... Jul 16, 2014 - 2:19 PM
Box Glad to see it looks like everything is fairly sor... Jul 16, 2014 - 3:10 PM
cardshark525 SO......... lol
Today as I'm pulling into my ... Jul 31, 2014 - 5:05 PM
enderswift There is a direct mechanical link fro the wheel to... Jul 31, 2014 - 9:37 PM
cardshark525 The coupler itself still rotates, but it physicall... Aug 1, 2014 - 11:39 PM
cardshark525 Took the vehicle to local Toyota dealership and th... Sep 4, 2014 - 3:41 PM![]() ![]() |
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