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![]() Enthusiast ![]() ![]() Joined Aug 27, '04 From Orange County, CA Currently Offline Reputation: 0 (0%) ![]() |
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This post has been edited by erics1one: Sep 22, 2009 - 11:15 AM -------------------- ![]() |
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![]() Enthusiast ![]() ![]() Joined Aug 27, '04 From Orange County, CA Currently Offline Reputation: 0 (0%) ![]() |
I know I've been running rich. Its never had a problem starting.
Well I can understand the need for a dyno tune to run at maximum efficiency, but why would it all the sudden get this huge bog down after no changes at all. The exhaust sounds like I'm a beefed up truck. Its been running good for about 6 months, and since I've never seen a hint of black smoke, I didn't think I was running rich enough to harm anything. It definitely sounds like something internal finally gave way. Guess I'll go NA and try to get my warranty to cover a swap. edit: Changed title from "HKS S-AFR, unplug or experiment" to "Barely stayin alive" since I'm not really asking about the AFR anymore. Even though this problem was going on before I unplugged it, I'll connect it back up, reset the ECU and see if I get anything different. This post has been edited by erics1one: Jan 26, 2005 - 10:55 AM -------------------- ![]() |
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Lo-Fi Version | Time is now: June 2nd, 2025 - 11:28 AM |