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Enthusiast ![]() Joined Mar 21, '04 From Oceanside Currently Offline Reputation: 2 (100%) ![]() |
I had a stud in the Exhaust manifold break at the head. In repairing it, my car is now pushing 12 pounds. I still have the stock ecu, no boost controller (until tomorrow), no FCD (stock max is 9.7). Now to give you a few more specifics: A friend of mine put a plastic t in my lines to trick the wastegate into allowing more boost. This caused me to reach 10 (probably 9.7, but meter isn't that detailed). In doing the repair I took the t out. I also found that my Cat was bad and took it out as well (it will cost me $300 to fix later). Replaced a crush gaskit after the stock down pipe to the 3" exhaust. Got everything together at approx 0130, and took it for a test drive. Found a couple of vacuum lines had worked themselves off of the stock BOV. Fixed those, and off again. Ran at stock 7 pounds of boost. Placed the t back in, ran at 10. Next day...got in the car got on it to pass a car...14! Took the t out, down to 12! It does seem to creep. When I hit the gas, it will jump to about 8-10, then steadily walk up to 12 as the rpm's increase. Did my wastegate go bad? I was thinking the increased flow in the exhaust from having no cat may have been the problem but it ran stock the night I did everything. Any ideas?
This post has been edited by Green_MachToy: Dec 5, 2005 - 8:34 AM |
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![]() Enthusiast ![]() ![]() ![]() ![]() ![]() Joined Aug 31, '02 From Philadelphia, PA Currently Offline Reputation: 8 (100%) ![]() |
server is up and running. .. www.celicatech.com then check out the list i made under the FI section in the 3sgte info stickie
once you find the post,scroll down and see the codes for the 1st, 2nd and 3rd gen motors This post has been edited by lagos: Dec 6, 2005 - 12:18 AM -------------------- 15PSI - 30MPG - Megasquirt Tuned
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Lo-Fi Version | Time is now: July 11th, 2025 - 9:41 AM |