May 14, 2011 - 11:45 AM
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![]() Enthusiast ![]() ![]() ![]() ![]() ![]() Joined Feb 11, '08 From Auckland, New Zealand Currently Offline Reputation: 0 (0%) |
Any suggestions? I want to run 16psi, the included actuator should be 12psi but its spiking to 20psi alot faster than i can let off the throttle
am going to pull the downpipe off and test the actuator with a pump, maybe change from 5mm hose to 8mm hose? (Mr Garry's actuator nipple seems a little bigger than Mr CT's) but has anyone seen this themselves and seen an effective fix short of going external? if my actuator and door are operating as normal, will porting the gate do the trick? any special tricks? This post has been edited by delusionz: May 24, 2011 - 12:18 AM -------------------- Mike W
1996 Toyota Celica ST205 GT-FOUR GT2860RS turbine, TiAL mvr44, JE 86.5φ piston, Clutchmasters FX400, APEX P-FC 269awhp / 273ft-lbs |
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May 24, 2011 - 12:25 AM
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![]() Enthusiast ![]() ![]() ![]() ![]() ![]() Joined Feb 11, '08 From Auckland, New Zealand Currently Offline Reputation: 0 (0%) |
Fixed overboost.
The wastegate hole was bored out an extra 3mm and the path on the inside was grinded out to direct more flow towards the wastegate instead of straight down to the turbine. Also the swivelling bracket was modified to bring the actuator arm closer to the pivot point so that the door opens wider. The standard actuator arm only moves so far, in effect the wastegate door opens about 45 degrees instead of 90 deg Now it seems to hang on to 0.9bar instead of shooting upwards of 1.4bar. I've lost alot of low end response and some midrange punch but I think this can be remedied with a better EBC. I haven't revved out to 7000 yet, So I'll update this later. If problems persist, the next step will be fitting either a 2.25" or 2.5" restrictor before the rear muffler -------------------- Mike W
1996 Toyota Celica ST205 GT-FOUR GT2860RS turbine, TiAL mvr44, JE 86.5φ piston, Clutchmasters FX400, APEX P-FC 269awhp / 273ft-lbs |
delusionz gt2860rs .64 rear housing overboost gen3 3s-gte May 14, 2011 - 11:45 AM
Culpable04 make sure to check the downpipe, sometimes the was... May 14, 2011 - 3:14 PM
delusionz started with my HKS EVC I hooked up, then tried by... May 14, 2011 - 4:28 PM
Rusty Is it an adjustable actuator? Try winding it out a... May 15, 2011 - 2:17 AM
presure2 creep is pretty common with the internal gated ... May 15, 2011 - 9:30 AM
korban Although i'm going to an external wastegate, i... May 15, 2011 - 7:18 PM
delusionz I dialed my HKS EVC to the 1.0bar marker and hoppe... May 24, 2011 - 10:22 AM
delusionz I only managed to push 5500rpm in 3rd gear otherwi... May 24, 2011 - 10:38 AM
presure2 excellent!!!
do you have any pics of t... May 28, 2011 - 9:10 AM
delusionz Nope.. done it again. I had a good trashing today,... May 29, 2011 - 6:05 AM![]() ![]() |
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